OSDN Git Service

switchtec: Remove immediate status check after submitting MRPC command
authorKelvin Cao <kelvin.cao@microchip.com>
Mon, 10 Dec 2018 09:12:20 +0000 (17:12 +0800)
committerGreg Kroah-Hartman <gregkh@linuxfoundation.org>
Mon, 27 Jan 2020 13:50:05 +0000 (14:50 +0100)
[ Upstream commit 526180408b815aa7b96fd48bd23cdd33ef04e38e ]

After submitting a Firmware Download MRPC command, Switchtec firmware will
delay Management EP BAR MemRd TLP responses by more than 10ms.  This is a
firmware limitation.  Delayed MemRd completions are a problem for systems
with a low Completion Timeout (CTO).

The current driver checks the MRPC status immediately after submitting an
MRPC command, which results in a delayed MemRd completion that may cause a
Completion Timeout.

Remove the immediate status check and rely on the check after receiving an
interrupt or timing out.

This is only a software workaround to the READ issue and a proper fix of
this should be done in firmware.

Fixes: 080b47def5e5 ("MicroSemi Switchtec management interface driver")
Signed-off-by: Kelvin Cao <kelvin.cao@microchip.com>
Signed-off-by: Wesley Sheng <wesley.sheng@microchip.com>
Signed-off-by: Bjorn Helgaas <bhelgaas@google.com>
Reviewed-by: Logan Gunthorpe <logang@deltatee.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
drivers/pci/switch/switchtec.c

index 5aaa4ce..ceb7ab3 100644 (file)
@@ -134,10 +134,6 @@ static void mrpc_cmd_submit(struct switchtec_dev *stdev)
                    stuser->data, stuser->data_len);
        iowrite32(stuser->cmd, &stdev->mmio_mrpc->cmd);
 
-       stuser->status = ioread32(&stdev->mmio_mrpc->status);
-       if (stuser->status != SWITCHTEC_MRPC_STATUS_INPROGRESS)
-               mrpc_complete_cmd(stdev);
-
        schedule_delayed_work(&stdev->mrpc_timeout,
                              msecs_to_jiffies(500));
 }